Fixit Log

Fixing and making things, what tools to get and what skills to learn, ...
jacob
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Re: Fixit Log

Post by jacob »

DW , who's the resident plumber, has done 4 cartridge replacements over the years: kitchen(2), bathroom(1)(*), shower(1). She uses youtube. IIRC, in one of the pics above, you showed a cartridge with a worn out washer with groove carved into it. Just replacing that washer might save the situation.

We've just been buying random cartridges ($5-10) each time. I didn't know one could get free replacements :o

(*) That one was a little hairy because of course the armature had been walled in (unnecessarily so) by tiles and mud AFTER it was originally installed, but cutting the hole a little larger, the whole thing came out from the front using a single wrench.

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Sclass
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Re: Fixit Log

Post by Sclass »


plantingourpennies
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Re: Fixit Log

Post by plantingourpennies »

I repaired the transmission of a 1984 Honda Commercial Lawnmower and put it back into service

Questions
-I ordered parts from Texas and Alabama, and had them shipped to Florida to keep a mower from 1984 in service for another 25 years, and saved significant money in the process compared to buying a new one. Was this repair as good for the environment as it was for my pocketbook, or would it have been better to get a new unit with better emissions technology? In automobile terms, my mower is one of the pre-emissions dinosaurs, belching smog wherever it goes. Units built after 2007 should have about 60% less pollution.

Lessons Learned-
-Buy commercial grade so that it is repairable
-When buying, consider the availability of parts, now and into the future
-If no diagnostic advice available on the net or shop manual, parts diagrams alone are enough to perform many repairs

Total parts cost-about 50$, 40$ in seals and bearings, about $10 in gear oil
Total time-about a week because of parts delay
Money saved-Nobody offers to repair these units anymore, buying a comparable new mower would be $800-1000
Tools required-Basic hand tools and metric wrench set

Living in the sub-tropical zone of Florida means I use a lawnmower at our house during the growing season. About 8 years ago I decided that buying an old, commercial grade unit made sense because it was designed/manufactured to be repaired instead of discarded.I chose Honda because they continue to make parts (gaskets, bearings, or entire rebuild kits) that are required to service these machines. I rebuilt the engine about 6 years ago, and the transmission stopped functioning at the end of last summer.

This repair was more difficult because there were no youtube videos, blog posts, etc that describe the symptoms I had. As it turns out, the mechanism was really simple and the issue was caused by diluted/worn out gear oil. After 25+ years one of the gaskets had worn out so the remaining gear oil was low, thin, and mixed with water in the transmission case. I replaced all the gaskets, filled the transmission with new gear oil and was back in business.

George the original one
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Re: Fixit Log

Post by George the original one »

ffj wrote:
Sat Apr 14, 2018 9:33 am
It's the thing on the left just hanging.
At a wild guess, I'd think a whole-house lightning suppressor. Probably has markings on the side we can't see?

Farm_or
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Re: Fixit Log

Post by Farm_or »

The plumbing pictures reminded me. I like to flush the water heater every spring. My electric heater is ten years old and still going strong despite our hard water and old pipes.

This time, the old pipes and debris loosened to plug the modern shower mixing valve. Upon disassembling, found that there are tiny quarter inch check valves with screen strainers on the inlets. The cold inlet was fine, but hot inlet plugged with debris. I simply removed the hot side check valve assembly altogether. Shower works better than ever.

Front loader washing machine bearings died. New bearings were about $15 with new seals too. Used my automotive bearing puller, press kit $70, to replace bearings and seals. About four hours job. Wish I would have done it same time as springs and shock absorbers.

92 celica front wheel bearing. Unfortunately, had to replace the spindle too $55. Bearings and seals $50. Bearing tool kit $70. Four hours job.

enigmaT120
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Re: Fixit Log

Post by enigmaT120 »

Huh. Did you break the spindle trying to get the bearing out? I think my Honda bearings are more than that, unless I never have to replace them.

Farm_or
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Re: Fixit Log

Post by Farm_or »

@enigma - The outer half of the wheel bearing undercut the spindle. Dealer wanted $200 for a replacement spindle. Found the aftermarket spindle from a machine shop in CA $55.I didn't price bearing or seals at dealer. I bought Timken and National brands, since I am very confident in their quality.

I am not as sure of the quality of Chinese bearings that I put in my washing machine. I searched for hours for a brand name replacement bearings and seals, but my washing machine must be too old or unpopular?

I inspected the replacement parts before putting them in and they appear to be of high quality. It helps immensely if they are installed properly with a press tool and ample oil and techniques. Many high quality bearings are damaged during installation by impatient hammer mechanics. I plan to give good review after running longer than six months.

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Sclass
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Re: Fixit Log

Post by Sclass »

Farm_or wrote:
Thu Apr 19, 2018 9:02 am

92 celica front wheel bearing. Unfortunately, had to replace the spindle too $55. Bearings and seals $50. Bearing tool kit $70. Four hours job.
That’s Scotty Kilmers favorite inexpensive car. I had an 88 Celica. That car outlasted my desire to keep it.

Some of the bearing tools are available free rental from Autozone. I repacked my Mercedes fronts a couple of months ago. I really wanted the seal drivers but I made do with a block of wood. Edit - just looked at some annular bearing presses online. Nice tool. Not free rented at Autozone.

Aren’t Timken made in China now?

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Re: Fixit Log

Post by Farm_or »

@sclass - It wouldn't surprise me if timken is made in China. The box it came in said USA, as well as the national brand seals. I hope that they continue their brand quality no matter where they are made.

Some companies protect their brand image vehemently, but others seem to forget all of their insistence on quality for different words describing greed. I think the internet has made it harder for manufacturers to cut corners without word getting out.

I have bias for brand names that I have had experience with, but there have been instances where I have been disappointed. In my 25 year manufacturing career, I've installed a lot of Timken bearings and don't know of a single defect. I've gone to a couple of their dealer sponsored classes and have been impressed with their emphasis on quality and details.

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Sclass
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Re: Fixit Log

Post by Sclass »

Did a front wheel alignment (toe and camber) on my car today. I noticed my tires had a little bit of wear on the inner edge of the tire. I had aligned my car a year ago but I guess I've been a slob bumping into curbs and parking space barriers at the super market. I had about 1/8" of toe out.

My two favorite precision tools for doing this are my cheap tape measure. I can get really good toe measurements alone if I use a thumb tack to tack the tape measure (through a tiny hole I drill in it) to the tire with a push pin. Once I have a good stationary datum I can measure the toe across the vehicle with about +/- 1/16". Just measure tread groove to tread groove on the leading face of the tire and the trailing face then subtract. Then I just adjust the tie rods.

I use these:
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Tack right through the tape measure like this to secure the tape to the tire tread. Make sure you have a thick tread or you may have more than alignment to fix!

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The camber angle is measured using a special straight edge that I brace to the diameter of the wheel. I measure the angle of the face of the wheel w.r.t. vertical with an iphone apps Bubble Level or Clinometer. Seems to work. The resolution on the display is 0.1 degree. I think it is pretty good because the measurement is very repeatable. Drift isn't as bad a problem as it used to be with these semiconductor gyro devices.

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I got in a big argument with some optics metrology guys at Hewlett Packard back in the day that this job was impossible without the precision optical tools at the tire shop. People from their interferometer division. Phooey. Amateur racers align their cars trackside like this all day long...especially if they have to drive their cars to the track via city streets. After watching a few people do it I put my twist of the thumb tack and the iphone app in as I went. It takes a little longer and I have to check my work when I'm all done after a test drive, so it is more time consuming than taking it to the shop.

But I don't have to listen to the idiot service manager trying to tell me that I need new sway bar bushings, ball joints, upper control arms, struts etc. when I know I don't (because I already replaced them myself). Saves a few bucks but really it saves me from dealing with the trade school grads turning the wheel adjustment screws on my car. Half of the time they say it is out of range and they cannot do it, or they make it worse which I verify by driving and DIY measurement.

edit - some images of my specific tool kit for toe measurement.

drill hole in tape measures to tack it to tire.
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Push pin tape measure to tire. I'm trying to measure from groove to groove on each the leading face of the tire and trailing face of the tire.
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Measure to the other tire. Pick a groove and surface. I like the groove surface at 64". Just be consistent.
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Use two Harbor Freight Tools tapes for convenience and subtract the numbers. The tapes are free with coupon.
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As for accuracy and precision, well, it isn't a laser, but I measured it again today since it only takes ten minutes. Still the same.
Last edited by Sclass on Mon Apr 23, 2018 8:19 pm, edited 1 time in total.

jacob
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Re: Fixit Log

Post by jacob »

Other than my half of our house, my excalibur scroll saw is the most expensive thing I own (not sure our car is worth this much anymore).

Today it died!

This is unfortunate, because it's my version of a 3D printer. I use it to cut all kinds of intricate parts out of all kinds of weird material(*) for this and that ... but 95% of the use is for making presents, etc. Still, the remaining 5% has saved me a bunch of monies.

(*) Wood, plywood, acrylic, metal, delrin, ...

There's a rocker switch at the front of the arm (see link above) that is used to switch it on an off. I don't have a foot switch. When doing fret-work the rocker switch might be used 50-200 times for a single piece. I did notice it failing to switch on once or twice shortly before it failed permanently (it's good to pay attention), so I figured that the problem was likely the switch getting gunked up. After all, it has been used thousands of times.

The internet gave me very little to go on other than the fact that it might be the switch but more likely the fuse. I finally managed to locate the fuse (cleverly hidden underneath/behind where the power cord goes in. I checked the fuse with my multimeter. All good.

I found the manual. Since this is a pro/semi-pro machine the manual came with exploded diagrams showing all the part numbers. It was not immediately clear how to get to the switch. However, the diagram showed that some of the bolts are actually spares (THANK YOU!) and which ones were likely holding it together. Five hex screws later, I had the plastic cover of the upper arm off. The speed control is a potmeter (no surprise) and the switch is a basic switch (no surprise). Very conveniently, it was not soldered together but could be pulled off as the cables going back to the controller board were crimped onto the legs.

I wonder, are the legs standard sized? Is there are crimping tool? (Sclass, Riggerjack?) Because ...

I briefly considered shorting the switch and ordering a foot-switch instead. I didn't wanna ghetto it because 110V runs in those wires. I could have cut the shoes off and connected them with a wire nut for a semi-permanent alteration. (I prefer my messing around to be reversible!)

Having pulled the switch out and tested it with the multimeter it was confirmed to be if not the whole problem then at least part of the problem (it's conceivable that the controller board would have been wrecked too?!).

I looked the part number from the manual up on google. There's a US supplier. $8+shipping

I looked the part number from the actual part up on ebay. Bingo! The actual part! I ordered 1 then 10 more from two different suppliers in China (hedging my bets) for $8 shipping included. Where would we be without Chinese internet entrepreneurs?

Since China-mail is slow and because I was desperate, I started inspecting the @#$@#$ switch some more. And saw a tiny hole underneath the switch where I might be able to blow in some compressed air. I always keep one or more cans of this stuff around. Most useful aerosol ever. This was after much blowing from the top and into the switch to no effect. ("That's what she said yesterday!?") However, checking with the multimeter (lowest setting measuring resistance) again, the switch appeared to be working again, so I reinstalled it.

And success! The saw runs again.

Tools used: Google, ebay, hex wrench, multimeter, canned air, thin bladed screw driver (to pry the switch shoe/connections off), and needle nose plier (to get them back on)

So now I have 11 spare rocker switches coming in via China e-post. Maybe I can resell them on eBay for $8- a piece :-P

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Sclass
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Re: Fixit Log

Post by Sclass »

Oh Cool. Wait, you bought 10 switches at $8 or at $0.80?

My neighbor was selling one of these scroll saws at a yard sale yesterday. Not as fancy as yours. It was Dremel brand. I was really tempted to buy it because he was selling stuff really cheap. But I've never used one before and I was afraid it would take up space as I didn't use it. I'll have to rethink it because I make a lot of little parts from wood and plastic too.

Glad you got it fixed for free. A few bucks of Chinese switches in a junk box may come in handy later.

My fix today is a Sonicaire toothbrush. I bought a big family pack because they were cheap per unit but I stored the unused ones in a drawer for years. SO said hers finally got anemic after using it several years and I broke out the new ones in the drawer. One didn't take a charge. Argh! :x :x :x and it was new!

If I had just charged it once a year it probably would have lasted. I figured I had a small crystal growing between the anode and cathode in its nicad battery. This is pretty common on these things. They'll short the battery internally and it cannot take a charge. I remember an old telcom sat engineer explaining the concept to me when I was a teenager. The good news is you can burn the short open with 12V across the cell. I had two cells in series so I cranked up my supply to 30V. I figured the brush was dead anyway so what did I have to lose. I had to crack it open by prying at its seams with a screwdriver.

It was ultrasonic welded together (rubbed furiously at the interface till the plastic melts together) so it really had to be destructively cut and pried.

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Then I hooked the + and - terminals to the 30V supply. Basically I "jumped" it.

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The status led started blinking. I put the mess in the charger and it took a charge overnight. Yay! :D :D :D Now I just need to put it back together and seal it so my toothpaste and drool don't short out the innards.

I sealed the seam up with bath silicone. Clamped it in a vice. Then wiped up the excess glue. I think I have a fix here. I'll know more when I try to brush my teeth tomorrow.

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Glue seam.

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jacob
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Re: Fixit Log

Post by jacob »

After fixing/modding my headphones that were held together with hot glue, I've really come to appreciate the concept. You put a few beads/lines on the inside rim with the glue gun and then use a hairdryer (close and high) to melt the glue. When you want to disassemble, you just use the hairdryer again.

SavingWithBabies
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Re: Fixit Log

Post by SavingWithBabies »

This past weekend, I finally got around to changing the oil on our sedan. It's been sitting all winter so I had to charge up the battery too (putting a battery tender on it next winter). The sedan is a newer Toyota and it has a canister oil filter. This is the first time I've changed one of those. I bought a special tool at the parts store for about $12. Getting the canister of the first time was a bit of a bear but luckily one of those old big 4 way lug wrenches fit on the end so I could get enough torque to free it up. It was a bit messier to change compared to using a fully disposable oil filter but not too bad and I think the second time will go smoother.

I also realized we drive our vehicles so little per year that we're down to annual oil changes on each instead of at a mile threshold. I like using synthetic and Mobil 1 goes on sale with a rebate every 6 months so I've started buying ahead of time. I also found a bigger filter that fits on our other vehicle so I can get another 0.5-1 quarts of oil into it. The nice thing about changing them by calendar is that it is predictable and I can do it when I want to -- so I'll probably move both vehicles up to do it in the fall before it gets too cold.

@Sclass I've read about doing the alignment that way -- I might just try this on our sedan. The inner edges of the front tires are wearing excessively (about the same on each side). I'm a bit disappointed as it is a fairly new car so having to align it seems odd to me but maybe it was never properly aligned.

That hot glue tip is ingenious. Definitely adding that to my bag of tricks. I love new (to me) techniques that use things you already have.

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Sclass
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Re: Fixit Log

Post by Sclass »

SavingWithBabies wrote:
Tue Apr 24, 2018 8:57 am
@Sclass I've read about doing the alignment that way -- I might just try this on our sedan. The inner edges of the front tires are wearing excessively (about the same on each side). I'm a bit disappointed as it is a fairly new car so having to align it seems odd to me but maybe it was never properly aligned. On a lot of economy cars toe is the only adjustment.

That hot glue tip is ingenious. Definitely adding that to my bag of tricks. I love new (to me) techniques that use things you already have.
Yeah, you could at least check the toe. Adjusting it is the next hoop. I was shocked my inner edges were wearing a year after I aligned mine but I am a spaz on the parking space stops. The car had so much momentum, even a little bump can knock things out. There are many other variants that use strings, carpenter levels, boards etc. that you can see on YouTube under DIY alignment. At least you can check if something is wrong.

I’ll have to remember the hot glue disassembly trick. Good one. Hot glue is awesome in that the fix is so fast.

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Sclass
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Re: Fixit Log

Post by Sclass »

Just finished reassembling a lawnmower engine. I’d heard about all these small engine repair videos and correspondence classes as a kid. I think my high school even had a class where you learned to rebuild a Briggs and Stratton mower engine.

So this month I was digging around in my mom’s garden shed and found a mower with a bad engine. I tore it down and rebuilt it only referring to YouTube videos. It is a very simple engine and really doesn’t require any instructions because there are so few moving parts. I didn’t realize Tecumseh motors was a casualty of the recession and no longer exists. I was still able to buy new rings and main shaft seals cheap online.

I think I’ll try to rebuild our wood chipper engine if this works out. I’m almost done. If you want to learn engine rebuilding an old lawnmower will educate you up to a point. If you buy an old mower at a yard sale the penalty of failure is nil.

You can learn how to remove and install valves, piston rings. I did some heavy honing using the Autozone free tool rental hone. I installed oil seals, new gaskets etc. it really is an easy way to learn mechanics. One level lower than a motorcycle. You can wet your feet for cheap without much risk.

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Sclass
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Re: Fixit Log

Post by Sclass »

the photos showing the mower, top end inspection and damage to the cylinder. Bottom end tear down. Honing process to remove scuffs and attempt to get cylinder somewhat cylindrical again. All this work can be done with inexpensive mechanics tools from China. A $28 set from Harbor Freight will contain all the screwdrivers and sockets required to take it down. The special tools like ring expanders, ring compressors and cylinder hones were rented from Autozone using the free tool rental program. Pretty low buck STEM education.

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Sclass
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replaced batteries in handheld vac

Post by Sclass »

This handheld vac has steadily gotten weaker and weaker. I liked it because the lithium ion batteries really packed a punch. Unfortunately it is five years old now and it doesn't suck...haha. So I found these cheap batteries online for vaping and installed them in place of the old ones. Simple soldering. Take photos to document the connections. Tear apart, then resolder. Good as new.

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new batteries

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solder in the connections and screw it all back together. Good as new. Fixed for $7 worth of batteries.

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Sclass
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Annoying broken car key

Post by Sclass »

Car key fell apart. The cheap plastic head fell off. Since these are special steel keys, not like the cheap copies from the hardware store that are made from soft brass, I decided I'd fix the key head.

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A little CAD CAM later...,

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cut one side,

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then the other.

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check fit and put two identical pieces together around key.

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gorilla glue

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ahhhh, thats better.

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Sclass
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Re: Fixit Log

Post by Sclass »

Fixed my garage door. My door was getting really slow and noisy. It buckled and popped as it went up using my old Genie screw drive opener. I took a close look at the door and it was cracking. As it opened it would buckle in half and make horrible popping noises. I almost called the service number on the little sticker some repairman had stuck to the wall by the opener switch. But I decided to check YouTube first. There were a ton of videos on how to fix a popping roll up door. It is a common problem on cheap doors. I just followed the instructions. No creativity here. I just did it like the video author.

After that I tuned up my motor box. There is a rotary sensor that quits if the door is opening too slowly. Mine was quitting and it turns out they go out of calibration and the clutch needs to roughed up to get some grab to it. Another YouTube video. Take the clutch apart and scrub it on the driveway to rough up the plates. Instant tuneup. Door is working great now.

And I kept the repairman out of my pocket. I hate those guys who leave stickers all over the place with their phone number.

Door with aluminum reinforcements. I got them at the 80% off clearance at OSH. Farewell OSH.

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Just bolted some channel and struts to the door skin with self tapping screws.

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Closeup of the cracks. With my struts there is no more buckling and popping. Its quite solid.

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Clamped some conduits to the door at the existing hinge bolts to add some stiffness.

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Cleaned the old sticky grease out of the carriage and applied fresh moly grease left over from a CV joint repair.

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Spending money averted! Works like new. Not bad for a 30 year old door and power opener motor. Genie screw drives are actually pretty durable. Who knew. Last year I retrofitted the silly radio/code electronics with some ebay hardware that uses a rolling code to prevent kids with scanners from opening the door for fun. For about $20 I brought the security up to date. Now the motor, screw and door are good for another few years.

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